Skymaster Forum  

Go Back   Skymaster Forum > Messages
Register FAQ Members List Calendar Today's Posts

 
 
Thread Tools Rate Thread Display Modes
Prev Previous Post   Next Post Next
  #7  
Unread 03-03-12, 11:10 PM
Skymaster337B's Avatar
Skymaster337B Skymaster337B is offline
Registered User
 
Join Date: Jun 2004
Location: New Mexico
Posts: 509
Skymaster337B is an unknown quantity at this point
I'm going to take the side of the FAA investigator...you must push up the power on the good engine to stay in the air.

NTSB Identification: NYC07LA187
14 CFR Part 91: General Aviation
Accident occurred Wednesday, August 08, 2007 in Chamblee, GA
Probable Cause Approval Date: 12/24/2008
Aircraft: CESSNA T337G, registration: N969CB
Injuries: 2 Serious.
Shortly after takeoff on a hot day, after the airplane was about 10 miles from the departure airport, the rear engine failed for undetermined reasons. The pilot turned the airplane back toward the airport, feathered the rear engine, and maintained front engine power at the top of the green arc of the manifold pressure gage, at 33 inches of manifold pressure. The airplane did not maintain altitude at that power setting, and to avoid houses and vehicles on the ground, the pilot performed a forced landing at a water treatment plant. During the landing, the airplane struck the top of a concrete structure, hit the ground, and became engulfed in flames. According to the owner’s manual, after an engine failure, the remaining engine power to be used isto be "increased as required." The published maximum power setting was 37 inches of manifold pressure at "red line," without any time limitations. A performance calculation indicated that at the existing ambient temperatures, and at that power setting, the airplane should have climbed at least 290 feet per minute. Additional references to the use of a 37-inch power setting, including performance calculations, were noted in the owner’s manual.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

The pilot’s failure to utilize all of the power available following an engine failure. Contributing to the accident were the failure of the rear engine for undetermined reasons.
Reply With Quote
 



Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

vB code is On
Smilies are On
[IMG] code is Off
HTML code is Off
Forum Jump


All times are GMT -4. The time now is 01:59 AM.


Powered by vBulletin® Version 3.6.9
Copyright ©2000 - 2025, Jelsoft Enterprises Ltd.